广东工业大学学报 ›› 2013, Vol. 30 ›› Issue (1): 18-24.doi: 10.3969/j.issn.1007-7162.2013.01.004

• 综合研究 • 上一篇    下一篇

武汉原状粉质黏土与其重塑土的试验对比研究(Ⅰ):试验结果描述

杨雪强1,刘文治2,刘祖德3,何世秀4,陈善雄5   

  1. 1.广东工业大学 土木与交通工程学院,广东 广州 510006; 2.云南农业大学 建筑工程学院,云南 昆明 650204; 3.武汉大学 土木建筑工程学院,湖北 武汉 430074; 4.湖北工业大学 土木工程与建筑学院,湖北 武汉 430068; 5.中国科学院 武汉岩土力学研究所,湖北 武汉430074
  • 收稿日期:2012-11-08 出版日期:2013-03-30 发布日期:2013-03-30
  • 作者简介:杨雪强(1966-),男,教授,博士,主要研究方向为岩土类材料的强度与变形的基本特性、深基坑、边坡稳定及挡土结构土压力等.
  • 基金资助:

    广东省教育厅科研基金资助项目(2008278)

A Contrastive Study of Natural and Remoulded Silty Clays in Wuhan(Ⅰ): Description of Experimental Results

Yang Xue-qiang1,Liu Wen-zhi2,Liu Zu-de3,He Shi-xiu4,Chen Shan-xiong5   

  1. 1. School of Civil and Transportation Engineering, Guangdong University of Technology,Guangzhou 510006, China; 2 College of Architectural Engineering,Yunnan Agricultural University,Kunming 650204,China; 3. School of Civil and Architectural Engineering, Wuhan University,Wuhan 430074,China;4.  Department of Civil Engineering, Hubei University of Technology,Wuhan 430068, China;5. Institute of Rock and Soil Mechanics, Chinese Academy of Sciences,Wuhan 430074, China
  • Received:2012-11-08 Online:2013-03-30 Published:2013-03-30

摘要: 以武汉沙湖粉质黏土为研究对象,首先借助于高压固结仪,对重塑土和原状土进行了室内侧限的固结试验;其次利用改进的应力控制式常规三轴仪,在不同的加荷路径和排水条件下,对重塑土和原状土分别进行了常规三轴试验研究,并对试验资料进行了较为系统的分析.结果表明:1)原状土的侧压力系数约为0.56,超固结比约等于1.2,为弱超固结土体,其结构屈服压力稍大于其前期固结压力; 2)原状土初始的切线模量及其抗剪强度均高于重塑土相应的值; 3)在固结排水条件下的三轴剪切试验,原状土的剪胀量要小于重塑土的剪胀量,但在固结不排水条件下,原状土体的剪胀趋势却明显要高于重塑土的剪胀趋势.

关键词: 原状粉质黏土;重塑粉质黏土;k0固结试验;三轴试验;剪胀

Abstract: Silty clay samples taken 9.5 m beneath ground level from Shahu in Wuhan were mainly tested. Firstly, the  high pressure consolidometer was used to conduct the k0 consolidation tests for both samples of natural silty clay and those of remoulded silty clay respectively. Secondly, stress controlled triaxial shear device was also used to test the samples of natural and remoulded silty clay along different loading paths under different drainage conditions. All testing data were analyzed and studied in detail. Experimental results show that: 1) natural silty clay is overconsolidated soil with OCR and lateral pressure coefficient being 1.2 and 0.56 respectively, and its structure yield strength is a little bit bigger than its preconsolidation pressure; 2) initial elastic modulus and shear strength of the natural soil are both higher than corresponding values of the remoulded soil; 3) for triaxial shearing under consolidated drainage conditions, the diltancy values causing volume increment of natural samples are usually smaller than the corresponding values of remtsiltoulded soil samples; but for triaxial shearing under consolidated undrainage status, the diltancy tendency for volume increment of the natural soil samples is more obvious than the corresponding diltancy tendency of the remoulded soil samples.

Key words: natural clay; remoulded soil clay; k0 consolidation test; triaxial test; diltancy

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